Posts: 837
Threads: 50
Joined: Mar 2014
Not yet, but soon. That is why I resorted to IR measurements
Jon Kabbe
1993 coach 337 with Civic towed
Posts: 2,718
Threads: 229
Joined: Jul 2012
Jon what I did was run an extension cord from the upper tv cabinet (hooked up to the inverter) down to the console compartment below the dashboard then use a small electric heater to take the chill off near my feet. At least that's what I think I remember doing and it might still be there.
But yes the dash heater never did put out much heat.
Forest & Cindy Olivier
1987 log cabin
2011 Roadtrek C210P
PO 1999 Foretravel 36'
1998 Newell 45' #486
1993 Newell 39' #337
Posts: 5,537
Threads: 260
Joined: Jul 2012
Jon,
You might think about a couple of other factors. The first would be potential leakage of cold air into the front of the coach while driving. In both coaches I have found significant air coming in. The second is the plenums for air distribution need some TLC after a few years. The foam seals inside break down, and I found that as built the plenum didn't work as it should.
I took it out, put it on the bench, and using a vac generator to actuate the motors, I was able to get air going where it was supposed to.
Richard and Rhonda Entrekin
95 Newell, 390 Ex caretaker
99 Newell, 512 Ex caretaker
07 Prevost Marathon, 1025
Maverick Hybrid Toad
Inverness, FL (when we're home

)
Posts: 5,776
Threads: 497
Joined: Jul 2012
i did something similar to richard only i didnt take it out. i used a hand vacuum pump and tried each louver that way. i found that the vacuum plumbing was goofed up and i changed it to make it work.
i also had to change the cable to the hot water valve up front and the dash control.
tom
2002 45'8" Newell Coach 608 Series 60 DDEC4/Allison World 6 Speed HD4000MH
Posts: 837
Threads: 50
Joined: Mar 2014
I rebuilt the butterfly baffle actuators when I installed an electric vacuum pump to replace the compressed air driven one. That made a huge difference in my compressed air consumption.
I had a huge outside air draft coming from 3 sources; a warped entry door which I rebuilt, air leakage into the box containing the heating system which I sealed with foam panels, and air leakage where the hoses from the heater box penetrated the floor which I solved by stuffing foam into the gaps. I could have sprayed foam in gaps but that would make future repairs more difficult. I found these air leaks by turning on all my vent fans and watching airflow with an incense stick, and checked that they were gone by using the same method after corrections. There is no way for the heater to keep up when there are significant air leaks.
I found one reference to coolant heaters for buses rated at 45,000 btu/hr that assumed 7gpm and 13 degree temperature rise. The usage end would then be 7gpm and 13 degree temperature drop. These numbers sound consistent with what I calculated, though my numbers were smaller because the core design is smaller. Then again I haven't been involved in heat exchanger design in about 30 years so I could be off (that has been said about me a lot).
Forest: The cord is still there and should I find a nice lady to travel with I suspect she is the one that will benefit from the electric heat
Jon Kabbe
1993 coach 337 with Civic towed